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  Reducer series
  JYT series bevel gear redirector
  SWL Series worm screw lift
  ZDY, ZLY, ZSY Series Hardened
  DBY, DCY, DBYK, DCYK reducer
  M series of large gear reducer
  HB series industrial gear box
  Gear Motor Series
  JYR Series Helical Gear Speed-Reducing Motor
  JYF Series Parallel Shaft Helical Gear Speed-Reducing Motor
  JYK Series Helical-Bevel Gear Speed-Reducing Motor
  JYS Series Helical-Worm Gear Speed-Reducing Motor
  YCJ-2 Series Helical-Worm Gear Speed-Reducing Motor
  YCJ Series Helical Gear Speed-Reducing Motor
  CJY Series Helical Gear Speed-Reducing Motor
  YTC Series Helical Gear Speed-Reducing Motor
  TY coaxial geared motors
  NGW-L-F Series reducer dedicated cooling tower
  Motor Series
  Y series (IP44) three-phase asynchronous motor
  YD series change-pole multi-speed three-phase asynchronous motor
  YEJ series electromagnetic braking three-phase asynchronous motor
  YVP Series Variable Frequency Motor
  YG series roller three-phase asynchronous motor
  YGP Series roller motor with frequency control
  YVPG Series Inverter Motor Roller
  Y2 series three-phase asynchronous motor
  YH series high slip three phase induction motor
  YZ series crane and metallurgical (cage) induction motors
  YZP series of metallurgical Variable frequency motor
  JG2 series three-phase asynchronous motor roller
   News

Reducer output shaft is too small the problem appears broken

Common installation problems reducer - gear reducer output shaft is too small the problem appears broken Apart from the gear output assembly concentricity is not good, resulting from other than the broken shaft reducer, speed reducer output shaft, if broken, nothing more than the following reasons. First, the error resulted in the selection of output with less gear. Some users in the selection, the misconception that as long as the selected gear of the rated output torque can meet the job requirements, and it is not true, first, the motor with rated output torque multiplied by the reduction ratio, the value in principle, be smaller provided in similar samples of the rated output torque reducer, and second, while also considering its drive motor overload capacity and actual work required in the maximum torque. In theory, users need maximum operating torque. Reducer must be less than 2 times the rated output torque. In particular, some applications must strictly abide by the guidelines, this is not only the protection of the gear reducer, the main thing is to avoid the gear was broken, the output shaft. This is mainly because, if the device installation problems, reducer output shaft and the load was stuck, and then drive motor overload will still continue to increase its output, thus, may be bearing reducer output force exceeds 2 times rated output torque which is broken, the gear reducer output shaft.
Secondly, the process of acceleration and deceleration, speed reducer output shaft torque in high-risk by the moment of its rated output if more than 2 times the torque, and this acceleration and deceleration are too frequent, then the gear will eventually off-axis. Given this situation the less, so no further description here.

 

 
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